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Restoration diary

Reports of restoration work on 50029 and 50030.

Announcement of working party dates and details of restoration work carried out at working parties.

Cab restoration and electricals update

Cab restoration and electricals update

Recent work in the cabs of 50030 has been concentrating on freeing off the power controllers.  Ian Kemp and Dave Rolfe have sprayed them liberally with WD40 and worked them backwards and forwards.  As a result they move for the first time since 1992, albeit rather stiffly in the case of no 2 end controller at the moment.  Andy Rowlands fitted, tightened up and reconnected the cables on the replacement set of contacts Dave had removed from one of our spare power controllers, to replace the set found to be broken during our freeing-off of the controllers. To achieve this you need to unbolt the plate that holds the sets of contacts so it swings away from the cams, and refitting the bolts that hold the plate is difficult as the contact springs keep pushing the plate away from the cams, which makes it not the easiest job when hunched up under the driver's desk and you need three hands!

The controller in no 2 cab is still quite stiff despite repeated applications of various lubricants, but the one in no 1 cab is much easier to move. If we cannot make them easier to rotate, we may have to look at removing the entire controller pedestals and dis-assembling them totally to see if the nylon bearings need replacing.

 

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Ian and Peter Carter oiled the main big end bearings and barred the engine round.  Andy Rowlands has also been working to refit the reverser air piston in the electrical cubicle of 50030.

 

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Work party report 5th October 2014

Work party report 5th October 2014

Ian, Pete and Dave spent the day unfastening the bolts to allow the main generator fan to be removed.  The fan is between the generator and power unit (but bolted to the main generator itself) and is normally hidden by the surrounding cowling. It sucks in cold air from under the body to help cool the gen and the cowling keeps the air circulating round the gen rather than blowing it all round the engine compartment. It has to come out to give access to the next layer of bolts that actually connect the engine to the generator. This proved to be a very fiddly task in the limited space between the fan and engine block.  Ian is seen proudly displaying his dirty hands after the day's work!

 
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I continued cutting and fitting the cubicle air circuit, with the same difficulties as before, today was the turn of the field divert contactors. The pipe itself is easy to bend and the olives go on fine, it's getting my hands and a spanner to the connections round all the cables that's the problem. I should have done these pipes first before cabling, but as ever, wise after the event.
 
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Work party report 21st September 2014

Work party report 21st September 2014
Dave, Pete and Ian disconnected and removed the four sections of airshaft round the power unit flywheel and bolted up the second intercooler, which Dave then painted. I continued cutting and fitting cubicle air pipes, removed the Z23 resistor and a now-redundant cable from it to the CU6, in preparation for fitting an electronic device in its place as part of the CU6 upgrade.
 
As we were packing up we were greeted by the sound of eight Rolls Royce Merlins as both the preserved airworthy Lancasters flew over Rowsley.
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Work party report 7th September 2014

Work party report 7th September 2014

Mark brought two of the refurbished KV10s, paperwork, test sheets and circuit diagrams up to site. After a test fitting they were removed once again! Dave, Pete, Ian and I hoisted one of the intercoolers up onto the ex-50008 power unit and bolted it in place. The other is ready to be refitted but needs painting first. Dave started making a hoist arm to be fitted on a corner of the container over the workbench. I started fitting the cubicle air circuit pipes, which was somewhat difficult with all the cabling in place, so if I ever do that again, the lesson is fit the airpipes before the cabling, then the cables wouldn't be in the way!

The new airpipes are just visible in the photo below, between M4, M5 and M6.

I discovered the air connections on the reverser air cylinder are a different thread to all the others, so I brought it home with me to take to the supplier I got the other fittings from to see if they can provide the correct-thread fittings for it.

 

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Work party report 24th August

Work party report 24th August

A good day on site today. Former regular working member Wes Needle joined us for today's workparty.  Since getting married and starting a family, Wes hasn't had much time to indulge his chosen hobby, but because they had taken a break in a holiday cottage not far from Rowsley, he was able to take a day to join us while his wife Keren and the nippers went on the train.

Dave Rolfe continued cleaning and painting power unit pipework, then he, Wes, Peter Carter and Ian Kemp finished overhauling one of the intercoolers and reassembled it. They also started unfastening one of the compressors on 50030 ready for it to be removed as there is an overhauled one ready to take its place.

 

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I located the fittings and tubing I had purchased some time ago to replace the air circuit in Repulse. There are different threads that have been used on these fittings at various times, so it was a bit of a gamble whether we had chosen the right thread, but fortunately when I tried the fittings in the motor and divert contactors, they screwed in fine. I had made a diagram some time ago of the routing and connections of the air circuit in 50021, so I am now able to copy it in Repulse. I also finished off connecting up the newly-fitted reverser in the electrical cubicle of 50030 with all its wiring and connections.  Even the weather was kind to us!

 

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